Maerskdrilling.com uses cookies for the purposes of statistical analysis, targeted marketing of our products, improving the friendliness and usability of our website, tailoring content to your interests and engaging with social media. By visiting our website, you consent to our and third party use of cookies as described in our privacy and cookie policy.

Maersk Resolute performs after reactivation

After its reactivation from warm stacking, Maersk Resolute showed stellar performance in the Dutch sector for TAQA, DANA and Petrogas.

Maersk Resolute performs after reactivation

During warm stacking, the rig undertook the 10-yearly Class SPS, multiple rig upgrades, Lloyds acceptance survey as well as proactive repairs. In this period, the rig used its own crew for a majority of the scope – and as a result the rig maintained its core crew during the entire stacking period. This has provided significant value to our clients,  with Resolute performing with a high uptime of 99.3% and a well NPT below 5%.

Read more

Interceptor xx.jpg
The advantages of using jack-ups for subsea drilling
Interceptor xx.jpg
Interceptor - Reliability & Efficiency
Developer.jpg
Mærsk Developer: Shell Floater of the Year 2018
Maersk Convincer 1.jpg
Maersk Convincer: Shell Jack-up of the Year 2018
Viking.jpg
Viking: Extended flow back operations in the US Gulf of Mexico