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Integrator: Diverter line modification

The Integrator Rig Team works actively with our clients to identify projects that can lead to safe and more-efficient operations.

Integrator: Diverter line modification

After the production platform arrived on the Gina Krog field, it wasn’t possible to complete the top hole campaign with the current design of the diverter lines on the rig.
The Integrator Team led a project to modify the diverter lines and identified a cost-efficient solution that resulted in a significant cost reduction for the client.

The implemented solution also resulted in reduced need for skidding operations, and saved time for the client compared to the original diverter line design.

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